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In site application for steam profile control using high-temperature nitrogen foam, oil production improvement and water cut decrease are obvious.
Despite the significant decrease of transmitted NRTI resistance there is no clear cut decrease of either the prevalence of TAMs or the T215 revertant substitions (figure S1).
In line, we found no clear cut decrease in the local expression of IL-1β and IL-6, even though these are produced by B cells, T cells and macrophages.
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The water cut decreased by 4.66% and the well group oil productions increased by 21% after the in-depth profile control treatment.
At the mean time, water cut decreased to 82%%.
After 6 month injection, residual oil saturation decreased from 52.8 to 39.6 %, and water cut decreased from 96.4 to 71.6%%.
At initial stage of production after layer recombination, the water cut decreases firstly and then increases gradually.
Daily oil production increases 4 tons, daily gas production increases 3293 m3 and its water cut decreases 12%%.
Oil production per day increases from 4.5 to 26.8 tons and its water cut decreases from 89.6 to 15.8%%.
Under the condition of constant pressure variation, the water cut decreases with the increase in injection production ratio.
Figure 11 shows that after injection of 1.15 PV water the oil cut decreases to 5% and the water cut goes to 95%.
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